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Tac 7/22 TDR (take down rifle)
3/31/09 This section will allow you to follow the progress of this gun from concept through the complete build.

I had this idea
while
recuperating from a recent surgery. The goal is a small, carbine sized,
light weight
action with
removable
air tubes, adjustable stock, and take down capability so the entire
thing
can be
stored in a small
case. The illustration above was created over a photo of the actual
action
pieces
below, and is
therefore
pretty much to scale. The grid is scaled to 1 inch per small box, with
the bold lines
every 12 inches.
Let the work begin...

What we have here
is basically two complete action prototypes. Both are barreled in .22.
The top uses
a Webley barrel,
the bottom a BSA barrel. I simply used what I had laying around to
start
with. The air tubes
use a foot valve
to close off the air flow when the tubes are unscrewed from the action.
The valve bodies
incorporate a pin
valve to open the foot valve when the tubes are then screwed on the
action.
One of the
actions has a
pension
for cutting the O-ring on the tube every 4th or 5th time the tube is
screwed
on, so I
will need to get
that figured out. I think a bit more of a chamfer on the throat of the
valve body will take care
of that though...
The bottom
action,
being the more complete, is now functional. I took about 50 shots with
it the other
day, and would
report
the power to be at approximately 18-20 ft/lbs. Still working on parts,
I could feel
the striker being
dragged along the top of the trigger sear, which made both cocking and
shooting
a bit on the rough
side. I have since re contoured both the sear, and bottom of the
striker,
and things
are much smoother.
A different valve spring brought the power up significantly, and I
think
it is close
to the 25-30 ft/lbs
I am after. With replaceable air tubes, shot count isn't an issue at
this
point. The air
tubes measure 12
inches in body length (not including the fill valve and foot valve).

A closer look at
the breech area. The separate loading probe, and cocking knob
will
allow a pellet to
be chambered without
cocking the action. Good for the way I like to hunt. Just barely
visible
is the little
trigger unit I
designed
for this action. It is two stage, and completely adjustable. The screw
protruding
is actually inserted
into the first stage length adjustment hole, and will be replaced with
a trigger blade
that will have a
through hole to allow access to the adjustment. I just needed something
to pull on to set the
trigger weight,
and test fire... This fit the bill without having to make the blade
yet.
I already know that
I will be making
new sear arms with a different leading edge shape, to ease cocking
effort.
I will want
the beginnings of
the stock and grip roughed out prior to cutting a trigger blade so that
I can taylor
it's placement to
my liking rather than try to shape the other parts to fit around the
blade.
Less work...
The few things I
did concentrate on for this build didn't change the way things look, so
no new
pictures just yet.
I spent some time firing the prototype action. After trying bunches of
springs,
I decided on one
particular striker spring. I then played with fine tuning the spring
spacing
and pre load.
I actually spent
a good deal of time trying very small changes in this area, and noting
the results.
Good thing it's
been staying light later into the evenings!
I also redesigned
and cut the foot valve assembly for the air tubes. The first ones I
made
used
a small o-ring to
help seal the tubes when they were removed from the action. I found
that
the
o-ring would
occasionally
stick to the exit port (maybe once every 20-40 times), and prevent the
action from charging
when the tube was screwed on. Normally backing the tube out, and
screwing
it back in would
solve the problem. Yes, the o-ring sits in a groove, and yes, I tried
lubing
the ring.
I also tried several
different sizes and types of o-rings, with similar results - for those
that may be
wondering. The other
issue I had with the design was that when the action was charged the
valve
stem of the air
tube could be heard rattling back and forth if the action was shaken. I
didn't think
either of these
conditions would win many fans, hence the re-design.The new assembly
doesn't
use
an o-ring, and
utilizes
a spring to hold the stem in place when the action is charged.
Last area of
attention
this week has been the trigger sear. I re cut several and am
waiting
for some new springs
to arrive to test them. My main concern in the re-design was the feel
during cocking the
action. My original design on the sear left a slight hiccup in the
stroke
just as the sear
was about to engage
the striker. I've cut a couple of different leading edges on the sear
to
test.
The goal is to
smooth
it out...
It is one thing
to
pick a gun up, and go out and shoot it. It is a whole nother ball game
to
not only be able
to decide what every aspect of that gun is, but then try to figure out
exactly how
to go about making
it work the way I want it too. Good thing I am stubborn!
4/4/09 - A bit of
frustration has crept it's way into this build. When I originally cut
the
trigger
units for these
actions, I did so without a striker spring, nor any trigger component
springs
in the action. The
pieces all look like they should work together, and they do... At least
on the
one action I have
functional. After assembling the first action, I have a fair number of
springs
to choose from for
the striker, and a fair number of springs for a trigger unit. But,
after
putting
this one together
and testing, it became clear right away that I was going to need a
stiffer
trigger spring.
I scoured my shop, and found one that works perfectly. Only problem is
that it
came from an
aftermarket
carb jet kit for a Kehin FCR carb off my motorcycle. And ... I only
have
one.
The feel is good,
the release is clean, and the weight is adjustable down to a decently
light
feel.
I really like it!
I ordered a bunch
of springs that I thought would be close to what I needed, but none of
them
worked. I found
a few more to try that should be here early next week, and jeez are they
expensive - just
to try. If they don't work it may lead me to designing and cutting a
different
trigger unit for
these actions. While unable to go to sleep last night thinking about
this
problem
I drew up a new
design. It will change the lever configuration and leverage ratios. But,
will also relocate
the trigger blades placement below the action. Something I am hoping
to avoid.
I'm not an engineer, mathematician, or technical wizard with a wealth
of
experience
under my belt. Most
of what I do is trial and error, with the emphasis on the error part...
I get that if I
keep at it, a year from now I will know a great deal more than I do
right
now,
but, this learning
procedure can be a pain while in the midst of it!
I was able to get
a few more parts started for the rest of the build, such as the parts
for the main beam
of the rear stock assembly, and the shell for the silencer unit. The
problem with the
trigger unit tempered my enthusiasm though...
On the bright
side,
the one action I do have shooting is working pretty well. I probably
have
a couple of hundred
shots through it already. Loading a pellet is smooth. I do like the
trigger feel on
this one. While I don't really have a grip to hold onto as of yet, just
pointing the
action seems to
place the pellet in a predictable location down range. I've been using
a set
screw in the top
of the breech to align the barrel end with, while giving me a rough aim
on target.
The discharge sound
seems consistent. While not being an accurate measure of performance,
it does give me
hope that I am at least in the ballpark.
4/8/09 - Several
samples of small springs showed up yesterday. I took a few minutes
during
the day to at least
try installing them into the trigger units to test, and found a few
combos
that
seem to work.
New trigger sears are in order though... There was still a decent
hiccup
in the cocking
stroke as the sears
clear a lip in the striker.
Early this
morning
I cut a couple of new sear arms to test, altering the shape of the
leading
edge.
I had basically
convinced myself that these trigger units are not going to work, and
that
I am going to
have to return to
the drawing board to solve the problems I am experiencing with them.
That
is
until I installed
a new sear arm. I stumbled upon pay dirt. The cocking stroke is now
nice
and smooth.
Sear engagement
is nice and positive, and the trigger can be adjusted down to a light,
crisp release.

So, at least now
I have a trigger group to work with. There are however a few other
things
that I have
been struggling
with that keep this build on the frustrating side. I am still trying
several
different
alternatives for
the foot valve assembly, and have thus far met with some pretty
disappointing
failures. I am going
to ponder this problem for a while before attempting another
alternative.
This means that
for the time being, I am going to build up one of the actions with an
air
tube that
won't be removable.
I'll come back to this problem at another time... and concentrate on
the
rest
of the gun for now.
In order to pull
off the complete build as I originally planed will require the design
and
execution
of many pieces I
have yet to design. To do the furniture, I will be making mock ups, and
creating
molds to cast
synthetic
grip and fore arm components, along with a cheek piece. I also want to
make the action
removable from the stock, much the way a shotgun fore arm is removable.
Push button, and
click type arrangement, so that take down will indeed make for some
small
components.
I am not real
sure
I have the patience to wait till I have the time to figure out, and
build
all
this stuff to start
shooting the gun, so I for sure will build up one of the prototypes in
a simplified
manner so that at
least I have something to continue shot testing with... I will probably
come up with some
sort of a stock
to drop the action in, so that it will be a complete, usable
alternative
to what I originally
envisioned in the
illustration at the top of this page.

I completed the
majority
of the machine work for the removable but stocks for the two prototype
actions. Length
of pull is adjustable by pressing the brass button and sliding in or
out.
Adjustments
are in .375"
increments
from about 12.5 - 15.5" - roughly. I haven't really measured
yet...
I will be
designing and making
a new pad assembly. I used one of my standard set ups to get the ball
rolling. I want
to make something a bit more tactical in appearance, with some more
angular
contours. I will
need to make a new mold for the pad, so look for that in the near
future.
I also want to make
the "wiper" at the front of the outer tube from a hard durometer rubber.
This will help to
keep any wiggle in the assembly down to a minimum, while also preventing
scuffing of the
final finish along the adjustment area. A mold will be made for the
"wiper"
as well...
4/21/09 - I had the opportunity the last couple of evenings to start roughing out the stock pieces.

At least now the
gun is starting to look more like the original concept illustrated at
the
top. Those that
are good at looking
at things the way they will be when finished, will be able to see just
how close it is
to the original
idea I had. The stock pieces are made out of walnut scraps salvaged off
the shop floor
that had accumulated
over the winter. Once I am satisfied with the the shape, fit, and
detail
involved
in the pieces, I
will need to make molds out of them for producing synthetic parts using
a two part
urethane resin.
The parts will be coated with a textured finish prior to the mold
making
process,
which will impart
a good textured finish on the cast pieces. The ridges will also be
added
to the
fore arm piece prior
to texturizing and making the mold. The easiest way to do it is by
simply
gluing strips of
cardboard to the wood with crazy glue, and because is looks like hell,
I will wait
till I am closer
to the mold making point to do so...
Other tid bits
still
being worked on and tested are trigger sears. I have been tempted a
couple
of times to scrap
this trigger unit, and design something new. Every time I get close to
that point
I try a different
sear angle, or shape, or length, etc... which breaths new life into the
unit. Note: I am
still using the
screw sticking down as a trigger blade...
To understand why
I contemplate changing the trigger unit,
you need to
understand
how picky I am about triggers. Everything I have tried so far has
worked.
Some have been quite
decent, but I feel it can still be better. I am so far satisfied with
the
unit
I now have working
in this prototype.
I am also working
on a few pieces that will make the action
itself easily
removable
from the stock with the press or pull of a spring loaded lever, and
latch
system.
I currently have
the pieces mounted on the other action. When I have them all figured out
and working properly
I'll get a set cut and fitted to the stock, and this prototype.
I've been
plinking
a bit with this action with just a red dot sight mounted on the scope
rail,
and will say that
I am so far pleased with the way the gun loads, cocks, and shoots.
Overall
length, with the
length of pull set at 14.5 inches, is 31 inches from the curve of the
pad
to the tip of the
muzzle.
4/23/09 I did a bit more work on the furniture parts...

Making molds is
difficult.
Everything will show up in a mold. A hair, sanding marks, even finger
prints
will easily
be captured in the resins used to create a mold. So, goes without
saying
that there will
need to be plenty
of work done to the various parts prior to the mold making process.
There
can be
no sign or trace
of grain left on the wood, or it will appear in the final cast pieces.
I'll get back to that
at a later time,
as my goal now is to just get the gun shoot able/usable. Which it
basically
is now.
I took
approximately
150 shots today with the 4X12 scope mounted in the picture. I started
with
a 4X scope, but
it was difficult to see where the pellets where hitting at 50 plus
yards,
after doing
a 30 yard zero,
so I switched out to the 4X12. Accuracy at 30 yards seems to be what I
expected out
of the BSA barrel
with no surprise POI drama to contend with. I was easily getting
somewhere
around 20 - 24 shots
off a 2700 psi fill, no problem. More testing will be done as things
come
together
more. For the most
part, I think the performance is right where I expected everything to
be.
I tried a
different
breech seal method on this action, with no seal on the pellet probe
itself.
I also wanted to
keep the seal easy to replace in the event of failure. I am for sure
getting
a little
blow by out of the
arrangement, so will need to redesign that set up. Worst case I will
simply
add a seal to the
probe, and go for a traditional set up there.
Last thing I will
look at in the next few days is the trigger, again. I have just the
slightest
hiccup in the first
stage travel to address. Second stage seems to be pretty good, and let
off is
real close to what
I am looking for. The hiccup could just be some dirt or debris in the
assembly.
There's plenty of
dust and grit on the work bench, and I am constantly having to clean the
actions out... Now
that the weather is coming around I can get the shop door opened up
and get a good
spring
cleaning done...
Prior to making
molds
for all the pieces I will need to produce any more of this action
I am going to dress
one of my prototypes in a charcoal laminate stock with ebony accents.
The action will
be finished off gloss black with polished aluminum bits for accents.
The
other
action will go into
either a walnut one piece, or perhaps a two tone walnut finished unit,
the
action black and
gold as in the original illustration.
4/24/09 - I think this pict kind of says everything that needs saying...

I spent 20
- 30 minutes walking around on the hill out behind the house, and this
was the result
of the shot testing
I did up there. I would have to conclude that it works pretty good. I
will
need to
get a real trigger
blade cut and mounted before I go again. That screw hanging down works,
but
leaves plenty to
be desired! Also, the shroud work comes next, as this little sucker is
loud.
4/29/09 - Enough beating a dead horse... I recut trigger units for the prototypes.

The one on the
bottom
was the original. So of course the one on the action, as well as the
unit
just below it are
the newer ones. While the original unit worked, it was finicky, and
somewhat
inconsistent. One
day it worked great, the next it hiccuped. One day it would handle
bumping
(actually smacking)
the action, the next day no matter how firm I made the adjustment, it
would
misfire when
bumped...
So, a new grouping now rides the bottom of the action. I am much
happier with this
unit. One additional lever, as well as longer length with more leverage
and
adjustment range
makes for a nice trigger feel. Glad I finally decided to do it!
I also reworked the furniture... Which is still raw and unfinished in the pict below.

I did dye the
main
beam of the stock with a transparent ebony dye, which allows the grain
to still show
through,
but adds a color difference between it and the other pieces. With a
black
action sitting in
it, I think it's gonna look pretty cool. The cheek piece was reshaped
as
compared to
the first one I
did. This allowed me to switch from high mounts, to low mounts for the
scope. I
also reworked the
breech/probe seal arrangement, which eliminated any blow by.
With the changes
to the wood, and the new trigger group, the gun is shooting quite well
now.
Next will be the
shroud work, a dust cap for the fill nipple and a trigger guard. This
will
pretty much
wrap up all the
major design and development work involved with this project.
With some additional
testing I would expect to start building more of these and the
Bullhead LRP pretty
soon.
If you've made it
this far down the page, you must still be interested. Pricing isn't
firm
yet, and will depend
on several options,
including caliber, stock material and degree of take down options, as
well
as type of finish.
I will be making
some of these with non removable air tubes (somewhere between 14 -16"),
some with removable
air tubes (12"), and some with quick detachable stocks.
I am not taking
orders
for these, just trying to judge interest, and get an idea of what to
build.
If you think
you may be interested in purchasing one of these custom pieces, give us
a call and we can
talk about it a
bit 304-273-0937, after 6pm est.
5/1/09 New trigger = Gooooood! I like it.
This little
fellow
made the mistake of making himself visible about 37 yards outside of the
shop door, while
I was working on a trigger guard for the action.

Shot was taken
off
hand. This little action has turned out to be 35.5" of absolute joy to
shoot.
At 48 yards with
the gun rested on a jug sitting on the table of my band saw, the gun is
producing tight
little clover leaf groups, with hardly a "pu-phoooot" type sound. The
pellet
strike is noticeably
louder than the discharge sound, at this point.
I carefully
stoned
and polished, as well as lubricated all the trigger components, as up to
this time I have
been using the action with pieces fresh from machining. Cleaning and
dressing
everything has made
an awesome difference in the feel, and it is just what I was looking
for.
I got an itch,
and
have decided to make one of these actions in 9 mm, just for kicks.
The air tube will
not be removable, and the overall length of the tube will be about 2.5
inches longer
than what I have
now. Stay tuned....
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